So this was the weekend i was to do my first test.
All i was waiting on was a piece of perspex for the top to replace the coreflute and off we go. Well again the perspex didn't materialise, again let down by someone else (but hey it's free).
Oh well what to do, i thought nah bugger it im still doing the test. Then the weather kicked in 38deg c one day and the same the next. I thought that there was no way im mixing resin in this heat.
My wife went to spotlight to grab some nylon material for the graphics, bought the one we saw the week before. I had all the resin and catalyst, the pump was finished, although no gauge yet and all the glass and plastic had been cut.
I saw a video from foamnfibr on youtube where he used pvc sheet for the top of his board with cotton and no breather or peel ply at all. So with not having that stuff yet i decided this was the way i was going to do it.
I didn't have a board cut out of foam or ply yet so this test was to see if i could make a top sheet.
So, with a top temp of 38 there was no way on earth i was going to try to do this on Saturday. Sunday morning came and it was around 630 am and about 20 degrees c. Yep its time.
So out to the garage i went and started to set things up. Oh before i go any further i decided to run two vacuum tubes from the table to the pump, why? who knows but here is how i set up the "T" piece. A brass tee with brass nipples. The 6mm tube didn't fit over it , i used some bigger tube, coated the edges with silicone and the same on the smaller tube and pushed it in to each blue tail till it stopped. I tested the seal and it worked great, no leaks anywhere in the whole system.
I have to say i was very nervous just before i was about to do this. But the one thing that doesn't scare me is fiber glassing. In the past i have re floored boats including mine, made a stitch and glue kayak and other laminated stuff with filler mixes and glue mixes. but every other time i had made stuff i had mixed with my own measurements, not very structured. This time i was going to use the correct amounts. I found a chart on the web whilst searching numerous sites , it shows the correct mix of resin and catalyst per volume. Good stuff.
http://www.acefibreglass.com.au/catalys ... 0guide.htm
I printed this out and used the exact amounts specified on it.
I poured out 250 grams of resin and put 3.8 mls of catalyst in the syringe as specified on the sheet.
Ok so here we go.
I laid out the first sheet of glass (cant remember the weight) and proceeded to pour about half the resin on.
So i wet the glass out. Above is the first layer wet out. I used an old credit card to do the resin spreading. In the past i have used rollers, foam brushes etc and i found the card especially for this job ( plastic scraper ) to be far and away the best, both for control of the resin and for getting it into the cloth evenly.
I didn't put down a resin layer before the cloth went down. This wasn't about getting a wiz bang finish, it was about getting things ironed out and getting confidant in the processes i would use in the future.
I was pretty happy with the first layer, a lot easier than i expected to be honest.
In time it is about 20 minutes into the job.
So down went the cotton. I used the scraper to spread it out to get rid of any creases ( not a lot of resin wicked through ( hmm a bit dry?). I laid down the last sheet of glass and poured the rest of the resin over it. I used the card again to spread the resin and found that the cotton had soaked up a bit more than i thought. I mixed up another 50grams and added some well measured ( guessed) out catalyst, about 1.5 mls. Geez id never used that little of that in my life. I spread it over the matting and made sure it was all wet. Above is the three layers before the plastic went over the top.
Ok time for the pvc. I rolled it out and realised that i had cut it too short, ahh crap. Oh well , i cut another piece and taped them across the far end. I then proceeded to tape the rest of the plastic down. The tape i used was normal duct tape.
I used some putty i had laying around to seal the tubes in each end and placed a piece of old cloth over each hose inlet under the plastic.
The big test was here. I was about 35 to 40 minutes into it, pretty good i reckon for the first time i had done this. The pump started and the pvc began to pull down. I had a leak around each hose either end. I mucked about and sealed those down without many worries. The close end in the picture really pulled down well so much so that you could see where it edged around the cotton, the other, not so .
Where i had joined the two pieces of plastic wasn't air tight, so i fooled around for about 15 minutes and got a good seal, but the far end still had a small leak somewhere that i just could not find. I put a separate patch over it and tried to seal where i heard some air. But it was pulling down ok so i didn't worry about it too much.
The pump didn't stop at all for roughly 4 hours, i was only going to leave it all on until it cured anyway. I was happy as it was a good test for the pump too.
When i felt the edges that had some built up resin that had hardened , i thought yep that's enough of that. It wasn't going to force down any more than what it had done already. I peeled of the pvc and to my surprise it just came straight off, not tugging or forcing at all. Just a firm pull.
When it came time to lift the sheet from the table i was totally surprised that it lifted of smoothly.
Well i was pretty happy with this first time effort. The finish is a smooth mat finish with a slight rib pattern in it from the coreflute board.
Where i had taped the two pieces of board together had a good shine in places. So when the perspex goes down , i have no doubt this sheet will be like glass. The sheet has a few little pock marks or voids but they are very small. There are no dry areas at all.
Soo, in the end i am very happy with how it turned out. It was a lot easier than i thought it would be to be honest. It took about 1 hour from setup to the final tape up and pump on and sucking.
There are a few things i would do different next time, but ill leave that for another time and have a bit more of a think. But as a test and first ever time doing this , i would give it a mark of 10/10.
As a finished pre cured top sheet ( well that's what it turned out as) i would give it a 7/10